TY - JOUR
T1 - Experiment and numerical analysis of catalytic CO2 methanation in bubbling fluidized bed reactor
AU - Ich Ngo, Son
AU - Lim, Young Il
AU - Lee, Doyeon
AU - Won Seo, Myung
AU - Kim, Sungwon
N1 - Publisher Copyright:
© 2021 Elsevier Ltd
PY - 2021/4/1
Y1 - 2021/4/1
N2 - This study experimentally and numerically investigated the hydrodynamics, reaction kinetics, and heat transfer of a bench-scale bubbling fluidized bed (BFB) reactor for CO2 methanation. A three-dimensional gas–solid Eulerian computational fluid dynamics (CFD) model coupled with a modified Syamlal–O'Brien drag model and reaction kinetics for Ni-based catalysts was developed. The CFD model was validated against experimental data for pressure, temperature, and gas composition at 1 bar and an inlet flow rate of 2 L/min with an inlet N2 content of 77.5%. The axial pressure drop, solid volume fraction, temperature, gas composition, and bed-to-wall heat transfer coefficient (HTC) were compared for four inlet N2 contents: 77.5%, 50%, 25%, and 0%. As the inlet N2 content decreased, the mean bed temperature increased from 340 to 456 °C, the gas volume decreased owing to the reaction, the fluidizing number (ug/umf) decreased from 4.1 to 3.5, and the solid holdup increased. Consequently, the HTC increased from 327 to 386 W/m2/K. This study identified successfully the effects of hydrodynamics and reaction kinetics on HTC in the BFB for CO2 methanation.
AB - This study experimentally and numerically investigated the hydrodynamics, reaction kinetics, and heat transfer of a bench-scale bubbling fluidized bed (BFB) reactor for CO2 methanation. A three-dimensional gas–solid Eulerian computational fluid dynamics (CFD) model coupled with a modified Syamlal–O'Brien drag model and reaction kinetics for Ni-based catalysts was developed. The CFD model was validated against experimental data for pressure, temperature, and gas composition at 1 bar and an inlet flow rate of 2 L/min with an inlet N2 content of 77.5%. The axial pressure drop, solid volume fraction, temperature, gas composition, and bed-to-wall heat transfer coefficient (HTC) were compared for four inlet N2 contents: 77.5%, 50%, 25%, and 0%. As the inlet N2 content decreased, the mean bed temperature increased from 340 to 456 °C, the gas volume decreased owing to the reaction, the fluidizing number (ug/umf) decreased from 4.1 to 3.5, and the solid holdup increased. Consequently, the HTC increased from 327 to 386 W/m2/K. This study identified successfully the effects of hydrodynamics and reaction kinetics on HTC in the BFB for CO2 methanation.
KW - Bubbling fluidized bed (BFB)
KW - CO methanation
KW - Computational fluid dynamics (CFD)
KW - Feed dilution
KW - Heat transfer coefficient (HTC)
KW - Power-to-Gas (PtG)
UR - http://www.scopus.com/inward/record.url?scp=85101343266&partnerID=8YFLogxK
U2 - 10.1016/j.enconman.2021.113863
DO - 10.1016/j.enconman.2021.113863
M3 - Article
AN - SCOPUS:85101343266
SN - 0196-8904
VL - 233
JO - Energy Conversion and Management
JF - Energy Conversion and Management
M1 - 113863
ER -